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Communication Dans Un Congrès Année : 2010

Experimental investigation of screech by an underexpanded supersonic jet with forward flight effect

Résumé

A coaxial supersonic facility has been upgraded in the anechoic room of the Centre Acoustique (LMFA, Ecole Centrale de Lyon) to reproduce a supersonic fan flow in forward flight. This paper first presents this new facility and some validation tests. A and B screech modes are characterized. Near-field microphones can well discriminate these two modes. A chaotic behaviour is found for mode B, which cannot be explained by mode switching. The effect of secondary flow on screech is essentially a decrease in frequency. Frequency jumps and hysteresis have also been observed with flight speed.
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Dates et versions

hal-00550554 , version 1 (28-12-2010)

Identifiants

  • HAL Id : hal-00550554 , version 1

Citer

Benoît André, Thomas Castelain, Christophe Bailly, Daniel Juvé. Experimental investigation of screech by an underexpanded supersonic jet with forward flight effect. 10ème Congrès Français d'Acoustique, Apr 2010, Lyon, France. ⟨hal-00550554⟩
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